My 1970 Ambo rockers seemed a bit noisy. So I pulled the rocker covers and started on the LH side.
When I pulled the cover, the intake rocker was pushed down, but the exhaust was completely loose. So for S&G I check the clearance on the exhaust, for the moment didn't care where the piston or cam was. .008" is what my flat feeler slid in at.
I rotated the crank to put the LH at TDC. Now the same valve was only .006. I remember setting the valves to In .004" and Ex .006". With the feeler gauge, they were .004: and .006" at TDC.
I checked the RH exhaust while the LH was at TDC and got .009". Have not rotated the RH to TDC yet, I'm assuming the same approximate numbers.
So......Is this a normal thing while not at TDC or is there a cam issue going on??
Thank you!
Tom