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Only seem to come on these days when I have a problem , which is a shame. True to form my Mille loves to come up with crazy issues, this one is a missfire that is on the LH cylinder only. The problem gets worse as the throttle is opened, At idle and low throttle settings below 3K RPM its hardly noticeable but give her any gass and its horrible, as the LH cylinder cuts out maybe 50% of the time. This is what ive tried.Cleaned both carbsChecked both Choke plungers are in good condition and fully closedChecked the needles havent climbed up the throttle springsCarbs kits recently applied (last 2 years)Fresh GasCleaned both fuel filters outRemoved the points and checked for play in DisyRemoved the points and retimedSwapped the coils, points, HT Caps, cut back the HT leads (leads less than 2 years old)Compression test 190psi cold 210 psi warmTappits checkedReally running out of the things to test. any ideas????Kev
Get a Dyna3 and quit chasing issues, this is my fix, the REST is just a waste of time & aggravation.
Could be a condenser, our did you switch them out too?
When you say you swapped the coils, etc., did you swap them from side to side or with other items? If you swapped them side to side, did the problem stay on the LH cylinder? If it did, have you tried swapping the carbs side to side ?
Can you put a timing light on the left cylinder and see if it’s electrical ?If you bring the revs up gradually in neutral, will the engine climb to high revs.5,000 rpm in neutral is only about 20% throttle, but in 5 th gear it’s closer to 70%. I want to know if the miss is a function of rpm or throttle setting.Not possible you have a sticking or mal adjusted valve ?
Totally concur.
Timing light is broken.Yes, if you have both cylinders. Pull the LH plug and the engine revs fine. Pull the RH plug and misfire is apperaent and it grows worse more throttle is appiled. Seems less effected by revs, so to me feels more fuel tan igintion.Sticking Valve would effect the compression? Compression is spot on.
Duff spark plug?
You could just disconnect the condenser on the bad side. Its there to minimize arcing across the points. A few minutes out of the circuit won’t hurt anything.Pete
Inlet air leak?Blocked exhaust?
Ohm your plug wires and verify their continuity. I developed a misfire on my pickup truck 7k miles after a new engine install, with of course all new ignition parts. I pulled my teeth out finding it until in despair I actually put the meter to the plug wires. One was so high as to be nearly an open circuit- that's the rub here, if you pull the plug or hold the wire to ground it will spark visibly in atmosphere but when you add the resistance of compression it will intermittently and increasingly fail to spark. The gap in my wire was nearly an inch long.
Soon as it gets out she turns into a stuttering mess.https://youtu.be/scKplrYKWvg
Many years ago my brother had a Yamaha DT250 which would run fine until it would just quit, leaving you wondering what was wrong . It would start again maybe with one kick, maybe fifty. I changed plug, condenser, points, retimed it. No good. Finally found the point wire was broken inside the insulation five or six inches back in the harness. It would just make contact then separate which caused the engine to quit.
I once bought a non running T that had been given up on. I found a small bare spot on the coil wire to the points that was rubbing on the frame. It had chrome bores so I wasn’t going to run it anyway so I was taking it apart when I found that. I found a half plugged idle jet on the other side. No wonder they gave up on it
I'll throw this out. In our outboard racing group we had 3 boats that could be rented to race. The purpose was to entice new people into the sport. At one point we had one boat that ran fine on the beach but when it went out on the course it would lose power and even die. I fiddled with it for quite a while but could find nothing wrong. I finally replaced the fuel line and all was good. Even though it flowed fine on the beach under full power it failed. I think what was happening was that ethanol in the fuel had broken down the internal part of the hose and it was being blocked with internal deterioration. Might be something to look at.kk