Author Topic: V1000 G5 Stator Removal (again))  (Read 6428 times)

Offline wirespokes

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Re: V1000 G5 Stator Removal (again))
« Reply #30 on: January 17, 2020, 09:35:12 AM »
I've removed caliper pistons with grease, but never would have thought of it for the rotor. Thanks for that trick!

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Re: V1000 G5 Stator Removal (again))
« Reply #31 on: January 17, 2020, 12:45:40 PM »
^^^^ Nice.. :thumb: I've removed blind bearings by making a punch that's a slip fit in the bore, putting grease in it, and smacking it with a copper hammer.

That is one way to remove the blind bearing in the front of a Mercury Outboard Quicksilver racing gear case.
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Re: V1000 G5 Stator Removal (again))
« Reply #32 on: March 10, 2020, 07:11:28 PM »
I have been trying to find a 8mm x 1.25 grease zerk with a longer threaded shank like this one that theoneandonlymin showed. All I can find have the short 1/2" shank.

Anyone know of a source?





That looks like a brake bleeder screw in the photo.
Charlie

Offline theoneandonlymin

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Re: V1000 G5 Stator Removal (again))
« Reply #33 on: March 11, 2020, 03:00:59 AM »
Sorry folks, my mistake.
It is a bleed nipple and I've made an international fool of myself so I have.

Cheers
Min

Offline John A

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Re: V1000 G5 Stator Removal (again))
« Reply #34 on: March 11, 2020, 09:18:55 AM »
You are in the right place,  I use this forum to make an international fool of myself on a regular basis
John
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Offline ozarquebus

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Re: V1000 G5 Stator Removal (again))
« Reply #35 on: March 11, 2020, 11:00:38 AM »
Hey that is great news. I have been tying to do the pump-off of my rotor with the M8 1.25 grease zerk and having a heck of time getting in on there. Also was looking in vain for an extended M8  grease zerk to no avail.

 So, the brake bleeder is m8 x 1.25 thread also?
John

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Offline ozarquebus

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Re: V1000 G5 Stator Removal (again))
« Reply #36 on: March 21, 2020, 11:01:57 AM »
At the risk of fully revealing my mechanical ineptness, I still haven't got my rotor off. I have used the pehayes extraction bolt as a center pull type of extraction method and am able to put sufficient pressure on the rotor to significantly flex the 1/4 in steel cross bar of the improvised puller.  I think I am exerting a sufficient amount of force for the rotor to come off, but no amount of 'heavy tapping' on the rotor bolt will free it. Front wheel is off and I can get a pretty good swing at it.
 To refresh everyones' memory on this belabored thread, I have jammed a too-soft, home-made extraction pin in the cam shaft/rotor center hole and cannot get it our or use the standard method of rotor removal.

 At this point I wonder how many turns of the screw are in the rotor and at what point does the screw engage the inner cam threads? I may be pulling on the whole cam instead of just the rotor, but am afraid of backing it off to just a couple of threads since I could possibly tear them out. I have tried a slap hammer, but the coupler was off center with too much flex. I am still in the process of making another fitting on that, but must re-borrow the slap hammer in the midst of social isolation.
 Additionally, in reference to the grease zerk pump off method, the grease zerk shank is so short and the recess in the rotor so deep and narrow, I am unsure of tighenting that down in there with a ground-down diameter socket will not produce another dilemma as well as being unsure if the pump off method is going to work, anyway. Does anyone know from what vehicle the brake bleeder valve pictured in earlier post that is 8mm x 1.25 came?
 I am almost to the point of cutting the rotor off with a dye grinder.
 
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Offline theoneandonlymin

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Re: V1000 G5 Stator Removal (again))
« Reply #37 on: March 21, 2020, 01:21:27 PM »
Yes , as far as I can remember I bought it from a VW restoration shop.

Cheers
Min

Offline chuck peterson

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Re: V1000 G5 Stator Removal (again))
« Reply #38 on: March 21, 2020, 02:13:47 PM »
crickets...ohh thats not good...maybe walk away for awhile

Speaking of embarrassing yourself internationally.. :grin:

I went one step worse and broke a tap in there...

But, who knew? Mcmaster-Carr had....drum roll...Tap Extractors for broken taps...received it the next day and rescued my a$$

Now, freaky ending if your still listening...about 3 years later I responded to a guzzi ad for a v700...great bike I bought it rode swapped it to jason speaker....but

We picked it up from the manufacturer of TAP EXTRACTORS (yes we supply mcmaster carr) from a tiny drill size to foot wide oil pipe tap extractors...beauti ful polished from age machine shop built by his grandfather...

What a world
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Offline John A

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Re: V1000 G5 Stator Removal (again))
« Reply #39 on: March 21, 2020, 02:22:48 PM »
at this point id think about making or finding a drill bushing and drilling it out with a left handed bit, maybe 1/8" or so. drilling a correct center will help you.  breaking off the drill bit will not.  tricky to get it on center with a hopefully soft rod wadded up in there.  go slow and clear chips more often than you think you need to.  normally there are threads, then no threads then threads again but I don't know their length . after you get a hole  hopefully on center , go bigger gradually until the piece will come out. the threads are harder than what you are drilling so that helps. I'm grateful I'm not doing that today but maybe you'll have good luck with it. keep the bit lubricated and clear chips with compressed air.
John
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Offline Cdn850T5NT

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Re: V1000 G5 Stator Removal (again))
« Reply #40 on: March 21, 2020, 06:32:27 PM »
I wish you the best of luck in getting it out. On a more general basis I wonder if the hydraulic means of extracting a rotor (on a bike that is not in this predictament) is actually the best/safest method; with the next safest the use of Rolf's hardened one-piece tool? The idea of using a separate rotor extraction tool, albeit hard enough to not bend... nevertheless goes a slight amount cock-eyed... whereas Rolf's tool does not misalign with the rotor threads.

Comments?
« Last Edit: March 21, 2020, 06:37:34 PM by Cdn850T5NT »
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Offline centauro

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Re: V1000 G5 Stator Removal (again))
« Reply #41 on: March 21, 2020, 07:05:15 PM »
I had the same issue on my SP a few years back; the removal tool pin that came with the bike's tool kit bent in the nose of the crankshaft, and the rotor would not budge. I actually rode the bike without the rotor bolt for months hoping that the centrifugal force would spin the dam rotor off..... But no, no joy with that, either; the rotor stayed on hopelessly stuck.

In the end, penetrating oil behind the rotor and tapping around its edge with a plastic mallet finally let it go. The bent soft pin will protrude from the crank nose about 1/4", enough to grip it with vise grips and yank it out.
But, otherwise, at this point, you may need a 3 jaw puller and a length of a hard steel round shank that will fit in the rotor hole on which the center of the jaw puller can pry against. You should be able to rent one for free at any auto parts store.
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Offline Chuck in Indiana

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Re: V1000 G5 Stator Removal (again))
« Reply #42 on: March 21, 2020, 07:16:10 PM »
Quote
But, who knew? Mcmaster-Carr had....drum roll...Tap Extractors for broken taps...received it the next day and rescued my a$$

You are a lucky man, Chuck.  :grin: Tap extractors are my "tool to break as a last resort before going to a carbide end mill or EDM."  :smiley: :smiley:
Chuck in (Elwood) Indiana/sometimes SoCal
 
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Re: V1000 G5 Stator Removal (again))
« Reply #43 on: March 21, 2020, 07:31:30 PM »
Don't know if this will help... The blade flange on old Lawn-Boy mowers fits onto a taper. No amount of pulling will separate them from the crankshaft (without destroying the flange). What works there is to loosen the nut holding the flange and blade to the crank, locking the crank from turning and then hitting the blade (still attached to the flange) one way or the other (clockwise or counter-clockwise).

If you don't mind destroying the rotor, the same could be done on a Guzzi, might work, I've never needed to find out if it does or not. Lock the crank from turning, use a chisel or punch against something on the outer circumference of the rotor, whack it with a big hammer.
Charlie

Offline John A

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Re: V1000 G5 Stator Removal (again))
« Reply #44 on: March 21, 2020, 11:57:38 PM »
It’s not time to drill until the rotor is off.  If you use a puller that the legs rest on the case be careful to not crack the case.  If there is some of the pin out the snout, your a lucky man!
John
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Re: V1000 G5 Stator Removal (again))
« Reply #45 on: March 22, 2020, 12:03:58 AM »
normally there are threads, then no threads then threads again but I don't know their length

OK, let us discuss the internal design here for clarification.

The removable rotor has a set of internal threads.  Normally, those rotor threads are not in use and don't do anything.

The nose of the crankshaft has more internal threads.  These crank threads are used to pull and hold the rotor in tight against the crank nose taper.

The rotor can fit onto the crank taper in any rotary position.  There is no keyway or process by which to precisely align the outer rotor threads and the inner crank threads.  Unless you were VERY lucky, it would be impossible to thread in very long bolt to engage both the rotor threading and the crank threading at the same time.  The slightest amount of rotation of the rotor on the crank nose would make the two sets of threads "out of timing" and the  long bolt would never work.  And if you did happen to get the threadings aligned, that would prevent the bolt from pulling the rotor inward differentially so as to engage the crank taper.

The original Guzzi bolt has a long narrow shank with a set of wider or larger threads at the business end.  How long is that set of threads on the factory bolt?  I don't know.  Someone with a bolt handy can measure.

So, there is an open, unthreaded space between the end of the rotor's  threads and the beginning of the crank's threads.  How long is that open space?  I don't know.  Easy enough to measure and extrapolate if someone else has one apart.  Most importantly, the length of the unthreaded empty space MUST BE longer or deeper than the length of threading on the factory bolt.  You can feel this when installing original parts.  The factory bolt threads into the rotor.  It turns and turns until suddenly  it goes through ALL of the rotor threads and pops free internally.  Now, push it in freely in the open space until it bumps up against the crank nose.  Begin turning again and those same bolt threads will now engage the crank threads and turn in until the bolt seats  home.

Unless you are not using a factory original bolt, it is NOT POSSIBLE to engage both the rotor threads AND  the crank threads at the very same time.  The empty space between is longer than the length of threading on the bolt.

The idea behind the factory hardened pin tool is to take up all of this free, unthreaded internal space. The factory bolt threads into the rotor but it abuts the extractor tool before it can pass into the unthreaded space.  Pressure on the bolt now forces the rotor off of the crank taper.  (We hope!)

So, take the tool I sent you.  Count how many turns of threading are on the end of that tool (which was made from a bent factory bolt).  Install the tool and turn it to engage rotor threads.  Count the number of tool rotations to match the number of thread crown count.  If it has ten thread crowns and you turn it in ten times you will have 100% of possible thread engagement contact.  Use the slap hammer and be bold.

I know the tool is bent or curved and that accounts for some slight 'shock absorbing' effect.  I know you currently have it set up with a rigged up 'puller'.  I would discourage the puller idea.  The removal from a taper is more dependent on SHOCK or IMPACT value than it is on raw FORCE value.

You have my sympathies.  I would  have thought it would be free by now.  OK to destroy the tool if necessary.  You could make another.  Just understand the relationship between the length of bolt threading and the length of internal rotor threading.  Make a bigger, harder, stouter tool but just match the threaded end length.

Charlie may have hit on a good shock idea (pun intended).  You seem to be prepared to destroy the rotor anyway.  How about huge Vice Grips on the rotor solid body.  VERY tight.  Then beat on the Vice Grips with a stout hammer in a rotational rather than linear fashion.  The crank, pistons, flywheel will all provide an inertial resistance.  Maybe  you can create enough rotation force to break the taper grip.  You could also 'lock' the flywheel with a stout screwdriver through the bell housing inspection hole.

I would resist the idea to try and CUT the rotor off.  IIRC, the back end of the rotor fits into a sealed hole in the timing chest.  Not exactly sure where you will cut off the rotor without damage to the crank nose.  You may end up with some portion still stuck on the crank.  Then you'd have to remove the timing chest cover to get at the remainder for further cutting.  UGH!

Keep us posted.  We're all rooting for you over the rotor.

Patrick Hayes
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Offline ozarquebus

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Re: V1000 G5 Stator Removal (again))
« Reply #46 on: March 22, 2020, 10:22:13 AM »
Thank you for that concise description of the thread situation, pehayes.
  Armed with the knowledge that I am not engaging the cam threads, I feel emboldened.
 When I get the slap hammer back with the new in line fitting fabricated to hold your extraction bolt, things are bound to give. If not, I'll try to twist the rotor off and replace it.
On my previous puller described I was using hardwood blocks against the case to prevent damage there, at least.
 Sorry for being such a pathetic cry-baby, but at least I walked away several times, as suggested here,  without resorting to dynamite and the mine hole in the back yard.
« Last Edit: March 22, 2020, 10:24:27 AM by ozarquebus »
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Offline wirespokes

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Re: V1000 G5 Stator Removal (again))
« Reply #47 on: March 22, 2020, 10:35:07 AM »
If you go the "rotate to break it loose" routine, consider a BIG F***ING pipe wrench. A strap wrench might be worth considering - that's something you could even make yourself.

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Re: V1000 G5 Stator Removal (again))
« Reply #48 on: March 22, 2020, 10:49:02 AM »
This is a big block motor.  The rotor is on the nose of the crankshaft, not on the camshaft.

A strap wrench is not likely to work.  Rubber or leather strap will absorb and attenuate the shock we are trying to transmit into the metals.  There is a chain version, but even that has flexibility that might reduce shock.  The pipe wrench is a good rotation idea.

Patrick Hayes
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Offline Chuck in Indiana

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Re: V1000 G5 Stator Removal (again))
« Reply #49 on: March 22, 2020, 11:07:52 AM »
Personally, if I didn't *care* about the rotor and all else has failed, I'd just take a big copper hammer and rap it sideways a few times. It definitely takes *shock* to break a holding taper. It's the same thing that keeps a drill chuck on it's arbor and that arbor in the drill's spindle. Pulling on a holding taper is pretty futile.
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Offline ozarquebus

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Re: V1000 G5 Stator Removal (again))
« Reply #50 on: April 25, 2020, 06:11:23 PM »
Eureka! The rotor is finally off. Using the pictured high tech tools, I beat on the rotor with hammer and a brass drift pin against the steel lobes of the rotor with rotational force with bike in gear. Also attached was the makeshift 'puller' improvised from a lawn mower blade, two hardwood blocks and Patrick's double-ender bolt pulling adapter. With tension applied, I hammered until the rotor made a full revolution taking up slack in the engine and drive train. As I was about to give up, I gave it one more might whack and " Kabong" the rotor and all the pulling contraption leapt off joyfully onto the wooden floor of the shed. the happy hooting and hollering was audible for a block by all the whole neighborhood sheltered in place.
 Visible in the picture is yet another home made bent extraction pin. I will say what everyone else has said that I failed to heed: either buy the cheap tool from Harpers or MG cycle or if you make it your self, make double sure it is hard tool steel and of the exact correct length and diameter.
 Removal of my rotor by striking it on its steel lobes has marred the surface of them, but appear to still be straight and the commutator is undamaged and it still has correct electrical continuity, so I guess I will re use it unless someone knows why I shouldn't.




 
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Offline Chuck in Indiana

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Re: V1000 G5 Stator Removal (again))
« Reply #51 on: April 25, 2020, 07:04:36 PM »
Sometimes "a bigger hammer" is the only solution.  :smiley: Congrats..
Chuck in (Elwood) Indiana/sometimes SoCal
 
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Offline Cdn850T5NT

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Re: V1000 G5 Stator Removal (again))
« Reply #52 on: April 25, 2020, 07:38:58 PM »
Glad you succeeded!
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Offline Furbo

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Re: V1000 G5 Stator Removal (again))
« Reply #53 on: April 26, 2020, 08:44:20 AM »
For a removal pin, I cut down a 5mm Allen wrench. Plenty hard and most of us have more than we need.

Did the same.  Just gotta make sure its a good quality steel. 
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Offline ozarquebus

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Re: V1000 G5 Stator Removal (again))
« Reply #54 on: April 26, 2020, 12:48:38 PM »
The actual method I used was due to my prior screw-up using a bad home made pin.

This guy in the video link below did it with a hardened bolt with the lower threads ground off.

Once you have seen how things are actually put together it becomes clearer.

The key for me was understanding there is a gap between the threads of the rotor and the threads on the crank and that you cannot really accidentally thread both with a single continuously threaded bolt.

I kind of like that idea better than inserting a pin that could get stuck, since the bolt still will be sticking out during use.

https://www.youtube.com/watch?v=9gvGtpn-GYM

Advice above from Patrick and Chuck above helped me a lot.
John

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Offline Cdn850T5NT

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Re: V1000 G5 Stator Removal (again))
« Reply #55 on: April 27, 2020, 06:08:44 PM »
I sure like the idea of Rolf Halvorsen's tool (extreme LHS in photo) for this job.  The notion of having a separate push-rod (which can go cock-eyed) after potentially mushrooming - gives me the heebie-jeebies.  One-piece makes more sense to me.  Also, prevents you from having to whack the head of the original Allen head capscrew.

One side of me would prefer a hex bolt... to Rolf's Allen-head... but I would NOT want to experiment / deviate away from a known working arrangement, that is to the say, the proven metallurgy / yield strength of Rolf's special tool.  Maybe put a piece of flatbar up against the Allen head, then whack on the piece of flatbar instead?







« Last Edit: April 27, 2020, 06:12:22 PM by Cdn850T5NT »
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Offline Chuck in Indiana

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Re: V1000 G5 Stator Removal (again))
« Reply #56 on: April 27, 2020, 06:43:37 PM »
You are over thinking it. Just put some pressure on the bolt, give it a whack with your copper hammer.. you *do* have one, right? and be prepared to catch it before it rolls off on the floor.  :grin:
Chuck in (Elwood) Indiana/sometimes SoCal
 
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Offline Cdn850T5NT

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Re: V1000 G5 Stator Removal (again))
« Reply #57 on: April 27, 2020, 10:06:08 PM »
Not sure if I have a copper hammer. Probably have a bronze one though in Dad's stash of tools I inheritted...
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Offline Old Jock

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Re: V1000 G5 Stator Removal (again))
« Reply #58 on: April 28, 2020, 04:20:48 AM »
I sure like the idea of Rolf Halvorsen's tool (extreme LHS in photo) for this job. 

I have it along with a few more of Rolf's tools, all of them work a treat.

Like a lot of things in life you get what you pay for

Offline ozarquebus

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Re: V1000 G5 Stator Removal (again))
« Reply #59 on: April 28, 2020, 08:07:37 AM »
Now that the rotor is off on my G5, I have been thinking through the failed previous attempts.
List of fails:

1. getting the bad pin stuck inside, FAIL
2. Using a large slap hammer with claw gripping the extraction bolt on the rotor FAIL
3. then using the improvised lawn-mower-blade inside puller. FAIL

I had managed to apply so much pulling tension against the rotor that the lawn mower blade was flexing at about 15 degrees. Hammered on the double nutted head of the pehayes extraction 'bolt' so much that 'had to change out the nuts, they were so beat up. 'thought for sure it would have come off then. Plenty of room to swing with a cat wif front wheel & fender off. I must admit, 'had no brass hammer and was using a short 2lb  iron hand-sledge.
I really thought that would have done it and was assuming at that point the rotor must be corroded onto the shaft.

SUCCESS: as described in earlier post, after getting off by beating it rotationally with puller, the shaft was inspected for corrosion: NONE.
It slick and shiny as new.

So lessons learned

1. Use good tool to start
2. Only moderate pulling force is needed if shock is effectively delivered.
3. An improvised INside puller of large mass largely damps the shock from the hammer
4. The taper fit is indeed very strong
5. There is a noticeable gap between the inside threads of the rotor and the inside threads of the crank shaft and it is unlikely to thread them both accidentally with an extraction bolt.
5. Though I would not normally recommend it, the steel lobes of the rotor are strong enough to carefully beat on some and rotor may survive if windings are not damaged and commutator area is protected.

thanks to especially to pehayes, cdn850, & chuckindiana

So i was wondering, is the brass hammer used to protect the bolt or does it deliver a more effective shock?
John

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